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EHS Performance

Doosan Infracore has strived to apply clean technologies to minimize air pollutants from production processes,installing pollution control facilities, using water-soluble paint and changing cutting oil. As a result, DI has acquired the ISO certification for the first time among companies in the same line of business. DI is promoting the continuous improvement of environmental performance.

Environment

Air

Pollutants created by our production processes include dust, THC (Total Hydrocarbon) and foul odors. To prevent dust created by the production of engine castings from being discharged into the air, we install and operate optimal preventive facilities to strictly manage pollutants at under 40% of the permissible level stipulated in the Act on Pollutants Management Standards. In particular, with the development of nearby housing lands and with the rapidly increasing population in mind, Incheon Plant conducted an external audit on our processes that may create foul odors in order to proactively respond to possible complaints from residents in line with the government’s policy on air quality improvement in the greater Seoul area. Based on these results, we, together with Incheon Dong-gu Office, drew up an improvement plan under which we are striving to invest in the installation of facilities designed to improve foul-odor-triggering processes and to apply eco-friendly processes.

Reducing Pollutants by Improving Hood

To resolve the structural problem of the existing Hood in the process of scrap metal, when charging scrap metal or taking out molten scrap metal, the double capture type is now used as it can capture pollutants very well. In addition, to improve the efficiency of disposing of the captured pollutants, the existing prevention facility was replaced with a high-efficiency prevention facility.

Reducing Pollutants by Improving Hood

Using Auto Pouring Machine to Reduce Pollutants

The auto pouring machine is installed for the manual pouring process to intensively capture pollutants and this reduces dust and odor in the factory. Also, the process automation reduces the risk of safety accidents likely to be caused by manual work.

Using Auto Pouring Machine to Reduce Pollutants

Using Concentrated Catalytic Oxidation (CCO) to Reduce THC

We installed the concentrated catalytic oxidation (CCO) system to reduce the THC from the coating process by more than 50% as compared to the old system. Also, we use a heat exchanger to recover waste heat, thus saving energy costs.

Using Concentrated Catalytic Oxidation (CCO) to Reduce THC

Reducing Pollutants from Coating Facilities

To reduce pollutants like THC and dust from the coating process, we installed a high-efficiency secondary pollution control facility below the existing pollution control facility.

Reducing Pollutants from Coating Facilities

Lowering of Flying Dust

To lower flying dust inside workplaces, now a big issue, we operate water-spray and cleaning vehicles twice a day across the plant. In the waste castings storage warehouse, we install and operate shed dust collectors and dust removal facilities using hoppers and piping systems.

Lowering of Flying Dust

Water

We clean and discharge all wastewater created in the production process by applying physical, chemical and biological treatment processes to the wastewater in the wastewater treatment plant. We automate the entire wastewater treatment process to manage pollutants at under 40% of the legally permissible level. In order to eliminate the environmental risk of contaminating the nearby sea water due to the plant site’s deposited pollutants being washed away during rainfall, we have installed and operated non-point pollutant sources reduction facilities designed to clean the rainwater via swirl-type systems and fiber-type filters that allow it to be discharged. We have also installed additional floodgates in general drainage ditches to fundamentally cut off the spread of pollutants attributed to unexpected leakage of dangerous goods.

Improving Wastewater Treatment Facilities

The new wastewater treatment facility of Incheon factory, with the addition of the biological treatment process and T-N removal process, reduced pollutants 50% more than the old facility. As we also installed monitoring systems like CCTV as part of the centralized management system, now real- time environmental monitoring and prevention of environmental accidents are possible.

Improving Wastewater Treatment Facilities

Monitoring Systems

We installed a warning system at all holding tanks in the middle to prevent environmental accidents, and installed the wastewater treatment monitoring system to quickly respond to emergencies. We also installed a monitoring system in four places vulnerable to accidents in order to prevent environmental accidents.

Monitoring Systems

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